This week for HTM(A)A, our task was to mill a wax mold positive, pour a rubber mold negative, and then finally create a positive out of a material of our choice!. First we needed a 3d STL file. Knowing that food was a good option for its unique textures and irregularities, I sided with the donut. Together me and him (or her?) would tackle this week's project.
To scan the donut, I utilized the 3d scanning techniques we learned 2 weeks prior. I even developed a high-tech donut jig to get photos of the underside (see above).Unfortunately, this failed to provide a decent model because 1) the hole (3d scan couldn't get in there!) and 2) the inability to capture the bottom of the donut.
After many attempts to scan a good model of the cake donut I purchased, I decided it would be easier to deform a Torus shape in rhino to get the "real donut" look I was trying to achieve. I did this with this free Rhino plugin called "Displacement"a>. It essentially allows you to distort the surface of any shape with a bitmap texture. Boom. Instant donut.
Since my block of wax was only going to leave 1/8" border around the rim, I wanted to make sure where the modela defines the origin. I did this by cutting a piece of foam and running a test job. It turns out it is at the centerpoint of the bit.
Here is the rough pass and final pass that I did on the modela using a 1/8" bit. This took about 2 hours.
The first half (mainly the finishing) took too long so I thought that maybe I could increase the stepover by decreasing the overlap by 0.4. The default was 0.9 and I moved it to 0.5. This caused a very poor resolution so I reverted back to 0.8.
After finishing, I realized that I had put the Bottom Value wrong for both my molds. I thought It was from the top of the material or -1 (Top value) to the base of your deepest cut (the registration holes or the non-model-base). THIS IS WRONG. The Bottom value should actually be the full height of the stl (negative value)...Otherwise it will scale your entire mill in the z direction and you will end up with shallow molds like these.
The depth of the negative should have been 3/4" but one was 1/2" and the other was 3/8".Well that was a nice 6 hours down the drain, so to save time I decided I ought to try the Shopbot. This ended up taking only 30 minutes (vs. 3 hours) per half donut. Shout out to James Coleman and Seto for teaching me how to generate my GCode in Partworks, and then to actually send a job.
Taking a picture or writing down the absolute bed origin will help in case the machine or program is turned off!
Roughing was done with a 1/4" flatend. This was about a 10minute job. Very fast
Here are the proper molds.
Note the depth versus the old incorrect ones.I used urethane as the negative mold material, the oomoo 25 was out.
The first and second poor did not go so well. This is because the first time I did not wait for the plaster and water to set. The second time (above), the plaster leaked out from the bottom, so nothing was left in the mold!
A little tape will do the job!