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Final Project


Final Slide - Link
Final Video - Link

Design Concept
The inspiration and concept for my final project design is discussed here on my Week 1 page. In general, my goal was to create a closed loop fluid circulating system that contained no pump seals. Below is a technical line drawing created in Fusion 360 of my design concept.


Using Fusion 360 I also created an amination of the model to better demonstrate how the system will operate.

The concept of creating a sealless pumping system is nothing new. They are commonly used in the medical and chemical fields in the form of peristaltic pumps. My design more closely resembles a mixing hot plate, which excites mixing by spinning a permanent magnet. The commercial pump vendor Levitronix is a leader in developing and producing bearingless and low shear pumping systems. These leverage more advance technology, but aligns with my original aim to fabricate a pump lacking a common failure component (e.g., bearings, mechanical seal, etc.).

After progressing in the semester, I filled in some of the interconnection gaps from my original design. This hand sketch depicts my excitation mechanisms, servo motor, and tank level indicator. I am sure this design will continue to evolve as I begin the fabrication process.

Pipe Coupling Fabrication
My initial coupling idea was to create a ring that would fit around the outside of both the fittings and the piping. Using a ShopBot in the RLE lab and its associated PartWorks3D program to generate tool paths, I milled a prototype ring out of plywood. I envisioned milling the actual rings out of Delrin to achieve a better surface for sealing, but I decided to pivot a different direction.


I liked my original design because it did not obstruct flow through the piping interior, but after realized that outer diameter of 2 in schedule 40 PVC piping was the same as my piping's inner diameter, I opted to fabricate sleeves that fit inside my piping and fittings. I viewed this as a time savings measure, because I would only need to machine one dimension of the sleeve (outer diameter to fit inside the fittings). I would accomplish this task using the lathe in the RLE machine shop.

The below images show my progression of machining. I took about 15 mils off the PVC pipe's radius to ensure my clear piping would fit over it. I had to take approximately 170 mils off the radius to ensure the fittings would fit over PVC coupling. All in all, this came together pretty well!



This is a time laspe of machining a few couplings.

Electromagnet Testing
Using a power supply to control current flow and a Hall Effect sensor, I tested a couple electromagnets. The first was an induction coil that I added an iron core to and the second was an iron core that I wrapped 26 AWG magnetic wire around. I was not satisfied with the strength of either of these arrangements, so I decided to research what drives induced magnetic field strength.

This is the formula I found for calculating the force induced by an electromagnet on a ferrous material. In this formula, ‘N’ is number of wire of turns, ‘I’ is current, ‘A’ is wire cross sectional area, ‘g’ is the air gap distance, and ‘mu’ is a magnetic force coefficient.

After realizing that the number of turns and current run through the coil had the greatest impact on magnetic field strength, I set out on making another electromagnet with more turns and heavier gauge wire that could accommodate higher amperage.

In addition to a permanent magnet these are the electromagnets that I testing while using a power supply to provide 1 A of current. In the above image, the coil to the left was used for tests 1 and 2, the middle coil was used for test 3, and the right coil was used for test 4. The results of my testing are shown in the below table. I was content with the performance of Electromagnet 4 and planned to construct more of them.

Wire Gauge (AWG) Coil Wraps Core Magnetic Field Strength (Relative Scaling)
Permanent Magnet N/A N/A N/A
>500
Electromagnet 1 20 150 Air
70
Electromagnet 2 20 150 Iron
150
Electromagnet 3 26 200 Iron
130
Electromagnet 3 18 400 Iron
300


Screw Impeller Design - 3D Printed
I designed my screw impeller in Fusion 360 using a coil to cut away from a cylinder. Using the hole function, I added holes for permanent magnet and small penetrates through the impeller’s thickness to assist with magnet removal. My CAD file is hyperlinked to the image.

I started off by printing a same segment of the screw to verify tolerances with the permanent magnets, shaft, and pipe. Once content with this print, I moved on to printing an impeller that made 1.5 revolutions. I anticipated this being my final print, but once I set the impeller on bearings within the pipe, I quickly realized it was not balanced. I would have to print in full revolution increments to produce a balanced impeller.

Test Section
Unbalanced Impeller

Print Iterations

Check Valve Development
Based on the inside diameter of my piping, I designed a check valve in Fusion 360. To ease 3D printing, I separated the check valve into three components, a valve body, plate, and flapper. My CAD file is hyperlinked here.

While designing the check valve flap, I realized that 3D printing with PLA may result in a component with a positive buoyancy; not what you want for a check valve flapper. After determining the density of PLA to be 1.25g/cm^3 I considered printing with 100% infill, but thought this was not a good use of materials or time. Instead, I brainstormed methods to add weight to the check valve flap. My first attempt to add weight involved pausing the mid-print to add small segments of all thread between the infill walls. After pausing the print, I failed to raise the extruder head from the component, which resulted in oozing of the surrounding area. This attempt, along with the oozing is shown below.


Turns out I didn't add nearly enough all thread to counteract the buoyancy of the component. My second attempt to add weight involved adding a hole to the topside of the flapper that I could insert pennies into. As shown below this was more effective.


Sadly, I encountered another issue with my check valve design; it failed to fully swing open because the shaft hole was not concentric with the hinge armature. The initial design and corrected design are shown below.

Initial Design
Corrected Design


Success! The valve now hinged open freely. I conducted a quick leak check of the valve and was content with its performance prior to adding a rubber gasket to the sealing face or grease/glue to seal between the valve body and the pipe.

Time to move on to assembling the check valve components. Using super glue, I adhered the valve body to the valve plate. I laser cut a rubber gasket to provide a better sealing surface and adhered it to the valve flapper. In the image to the left, the valve body is orange, the valve plate is yellow, and the valve flapper is white.

Turns out the rubber gasket idea didn't work out well. The additional thickness of the gasket prevented the valve flapper from seating properly on the valve plate. I could have extended the hinge height on the valve plate to account for the additional thickness. Instead using a Q-Tip and acetone I smoothed the 3D printing lines on both the valve flapper and valve plate sealing surfaces to create a better seal.

Finished Check Valve Assembly (No Gasket)

Exciter Disk Fabrication
I did a little math prior to fabricating my exciter disk. The below image shows my calculations for determining disk diameter. In general, I aimed to match the lateral magnet spacing of my screw impeller and exciter disk. I selected to use eight magnets to increase the rotational speed of my impeller.


I created my exciter disk design in Fusion 360. The CAD file is available here. Prior to laser cutting the disk, I did a test print of the hole cut out for the motor shaft. I was extremely pleased with the press fit tolerance of the motor shaft, so I proceeded to cut three disks using 1/4 inch acrylic. After laser cutting, I sandwiched the three disks together with super glue to create a disk of adequate thickness for embedding 1/2 inch diameter permanent magnets. Next, I used the Acer mill in the RLE machine shop to create 1/2 inch by 1/2 inch holes for embedding the magnets.


Board Coding
The codes for my motor and breakout boards are fairly simple. The motor board receives inputs from the potentiometer and Hall Effect sensor to control motor speed. The breakout board microcontroller receives an input from the Hall Effect sensor that activates a servo motor to open a drain valve. The codes are hyperlinked to their respective images.

Motor Board
Breakout Board

Testing - Round 1
I used hot glue to assembly my piping but left the pipe section containing the impeller unglued to allow for disassembly. Knowing these connections would not be watertight, I used my sandbox bin as a containment pool.

This testing was a pretty big disappointment. I was only able to achieve about a 1 inch difference in head pressure between my inlet and discharge pipe sections. I would need to increase torque of my impeller to increase head pressure, so I searched for alternate DC motors.

These are the DC motors I acquired for testing. The two on the left were used in the testing shown above. I planned to use the right two for future testing. The left motor was rated to be operated with 5 V. Both of the center motors were rated to be operated with 12 V. The one on the far right is from a 24 V battery powered weed wacker. All four motors have gear reducers.


I had used my motherboard without issues for the past couple of weeks, but suddenly started experiencing issues with the microcontroller. These issued stemmed from two sources. Initially, I was using the board to power a 5 V motor, but transitioned to using a 12 V motor that I powered externally via a power supply. My diode protection circuit was no longer dumping back to the motor's source voltage (12 V), but instead it returned to the board's source voltage (5 V). Additionally, I was powering the potentiometer with 5 V, which returned 5 V to the microcontroller at its highest setting. Both of discrepancies resulted in burning up a few microcontrollers, but after performing a little board by routing the diode protection to a jumper connection and manipulating the VCC trace for the potentiometer, I no longer experienced issues.

Gutted Board
Fixed Board

Keeping ferrous metals submerged in water is never a good idea, but I did not expect my bearing to begin deteriorating within 24 hours. At this point I considered turning my contraption into an auger to move plastic beads. I experimenting with this and quickly realized my design would require significant modifications to make this work, so I swapped out to a new pair of bearings that I coated with oil prior to installing.


Testing - Round 2
Prior to proceeding to my second round of testing I had to modify my motor bracket. I accomplished this by using a hole saw.

Dry Test
Wet Test

Everything ran well during the dry run, so I decided to give the wet test another run. With the new 12 V motor I was able to achieve a rise of 1.5 inches on the discharge side. Combined with a drop of 1.5 inches on the suction side, this test run achieved a total head difference of 3 inches while running at 12 V and 2 A.

Running the motor beyond 14 V resulted in the exciter disk over torquing and jump magnetics on the impeller. To increase torque between my exciter disk and impeller I narrowed the gap between the two by deepening frame notches with a file.

Final Assembly
I started by assembling my tanks and the actuator assembly for my drain valve. I used fishing line for my magnetic float to ride up and down. The fishing line worked, but it was a little stiff to allow for free motion, so I may swap to thread for the final presentation.


Next I assembled the frame for my tanks. I added bolts to each corner of the frame to allow me to adjust the height to fit the piping system. I drilled under sized holes, so the bolts would thread into the wood.


After full assembly it was time to conduct my final round of wet testing.

Project Evaluation
Overall, my sealless impeller does not perform as well as I would have hoped. By only achieving a head pressure of 3 inches I was not able to stack the tanks on top of each other. Instead, I had to stack the tanks side by side. I did not expect my drain valve to seal perfectly, but was disappointed that I had to replace it with a manufactured valve. I also ran out of time on fabricating an electromagnet excitation mechanism, which is why my frame is sparse on one side. However, I can confidently say I learned a tremendous amount throughout this course, more than in any single course I had taken prior. Thank you!